1399 Commits

Author SHA1 Message Date
Julian Oes
1a21dcd34d ESC calib: low PWM value was not set 2014-01-02 08:28:33 +01:00
Lorenz Meier
5b302fef59 HOTFIX: Increased attitude control updates to 50 Hz - was less than 10 Hz and unintended slow 2013-12-31 14:47:01 +01:00
Lorenz Meier
0153e334ff Add note about multi-port support on GCS side 2013-12-29 12:03:35 +01:00
Lorenz Meier
87a61de670 Support for more than 8 output ports 2013-12-29 12:02:23 +01:00
Lorenz Meier
01be817c59 Allow N comparisons of a param value, returns success if one matches 2013-12-28 22:14:28 +01:00
Julian Oes
e462c70af7 Merge remote-tracking branch 'px4/master' into control_groups 2013-12-27 23:57:37 +01:00
Julian Oes
020c47b59f PX4IO driver: even compiling now 2013-12-27 23:57:24 +01:00
Julian Oes
a4a5eee08d Attitude_estimator_ekf: Fix params, this bug caused the multirotor_att_control to stop 2013-12-27 23:27:25 +01:00
Lorenz Meier
f44f738f0a Fix return value 2013-12-27 21:56:54 +01:00
Lorenz Meier
965a7a4f03 Allow to disable a channel 2013-12-27 21:33:19 +01:00
Lorenz Meier
a9ea39054d Working around creating an error condition with more than 8 raw RC channels 2013-12-27 21:19:04 +01:00
Lorenz Meier
cddbb0d23f Merged master 2013-12-27 21:12:51 +01:00
Lorenz Meier
dd5549da46 Hotfix: Better dead zone defaults 2013-12-27 15:50:28 +01:00
Lorenz Meier
c5ef295f68 Hotfix: Reduce mag influence on att estimate 2013-12-27 15:46:50 +01:00
Lorenz Meier
d5c857615b Pure formatting cleanup of drv_hrt.c, no code / functionality changes 2013-12-27 12:14:15 +01:00
Lorenz Meier
db46672bc4 Paranoid PPM shape checking 2013-12-27 12:02:57 +01:00
Lorenz Meier
8d2950561d Changed RSSI range to 0..255 2013-12-25 15:15:15 +01:00
Lorenz Meier
edffade8ce Added PPM frame length feedback in IO comms and status command - allows to warn users about badly formatted PPM frames 2013-12-25 15:11:48 +01:00
Lorenz Meier
a502332992 Greatly robustified PPM parsing, needs cross-checking with receiver models 2013-12-25 15:11:05 +01:00
Thomas Gubler
c191597625 HIL: only listen to first 8 actuator outputs 2013-12-24 15:15:39 +01:00
Lorenz Meier
107bb54b33 Robustifiying PPM parsing 2013-12-23 20:38:09 +01:00
Lorenz Meier
64ad3d7e0a Added channel count to log format 2013-12-23 18:44:07 +01:00
Lorenz Meier
f617689094 Merge branch 'master' of github.com:PX4/Firmware into control_groups 2013-12-22 21:13:11 +01:00
Lorenz Meier
1279b5fbf3 Merge pull request #556 from PX4/ppm_parsing
PPM channel count detection is now using a more paranoid approach.
2013-12-22 12:13:02 -08:00
Lorenz Meier
f8134c9c67 Enable 18 channels on IO 2013-12-22 21:12:31 +01:00
Lorenz Meier
9abf31c2ba Support 18 channels correctly on FMU 2013-12-22 21:09:47 +01:00
Lorenz Meier
6c990d0a6e Fix usage of wrong constant for RC input channels 2013-12-22 20:44:51 +01:00
Lorenz Meier
999051546a Fixed compile error 2013-12-21 19:08:52 +01:00
Lorenz Meier
b84c9f962b Merged master 2013-12-21 19:07:24 +01:00
Lorenz Meier
831f153b73 Add tight RC test 2013-12-21 16:37:45 +01:00
Lorenz Meier
b2e527ffa6 Counting channel count changes 2013-12-21 16:13:04 +01:00
Lorenz Meier
3e037d40de Fixed bracketing error 2013-12-21 12:46:06 +01:00
Lorenz Meier
0f0dc5ba06 Allowed custom battery scaling on IO 2013-12-21 12:45:04 +01:00
Lorenz Meier
f174ca3ce5 Added average as direct output 2013-12-20 21:52:10 +01:00
Lorenz Meier
3ad9dd030c Added performance counter for write IOCTL 2013-12-20 21:10:33 +01:00
Lorenz Meier
8c518aa237 Useful bits for high-rate logging 2013-12-20 14:25:35 +01:00
Lorenz Meier
9476ba522f PPM channel count detection is now using a more paranoid approach. 2013-12-20 08:48:51 +01:00
Lorenz Meier
6dce57170e Hotfix: Fixed mapping of override channel 2013-12-19 17:12:46 +01:00
Lorenz Meier
b9a533acae Merge pull request #505 from PX4/rc_failsafe
Futaba RC failsafe support
2013-12-19 07:41:25 -08:00
Andrew Tridgell
bccf65cc28 mpu6000: disable interrupts during initial reset
this seems to avoid a problem where the mpu6000 doesn't startup
correctly if other devices are transferring at the same time.
2013-12-16 15:06:45 +01:00
Lorenz Meier
d53b00283e PX4IO upgrade improvement 2013-12-16 12:02:01 +01:00
Lorenz Meier
f4ac204f46 Cranking up bus speeds for all sensors to achievable 10.4 MHz, will cut the bus lock time to half 2013-12-15 18:32:46 +01:00
Lorenz Meier
d6a6d59d2d Further improved S.Bus scaling 2013-12-14 15:09:20 +01:00
Lorenz Meier
ea10d55d71 Auto-update of IO firmware, shorter preflight check alarm 2013-12-14 15:08:56 +01:00
Lorenz Meier
10b2dc67e4 Allow forceupdate in all conditions 2013-12-14 14:54:02 +01:00
Lorenz Meier
00dc339d2e Improved S.Bus scaling based on scope measurements 2013-12-14 14:52:57 +01:00
Lorenz Meier
9883a346a0 First stab at implementing better RSSI based connection status estimation, still needs some work and testing 2013-12-13 18:01:55 +01:00
Holger Steinhaus L
a673fa3926 Non-destructive handling of failsafe signals, distinction between frame loss and signal loss.
This kind of handling might be moved upstream into the application, once alarms are propagated by the ORB system.

This change is compatible with RX failsafe settings, but does not rely on it (uses SBus flags instead).
2013-12-13 17:30:26 +01:00
Holger Steinhaus L
3a40ea8338 more precise range conversion for SBus input signals 2013-12-13 17:30:14 +01:00
Lorenz Meier
0b9b68f0d9 Merge pull request #535 from NosDE/master
Device renamed, custom device on parameter switch
2013-12-13 08:10:57 -08:00