22816 Commits

Author SHA1 Message Date
Beat Küng
8b64fc8a5e Tools/px4moduledoc: add some comments, describe the regexes 2017-07-14 11:57:11 +02:00
Beat Küng
8a83fb7dc2 land_detector: use ModuleBase & add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
8d7481f9ac load_mon: use ModuleBase & add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
5aa8b455c2 crazyflie airframe: add maintainer 2017-07-14 11:57:11 +02:00
Beat Küng
69f0288649 aerofc airframe: RTF -> Ready to Fly Drone & add maintainer 2017-07-14 11:57:11 +02:00
Beat Küng
a63699060d ekf2: use ModuleBase & add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
47073e9c32 vmount: add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
28e5268497 dataman: rename to .cpp & add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
682dabded1 replay: use module base class & add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
674ae5292e markdown module doc script: write how to generate the modules documentation 2017-07-14 11:57:11 +02:00
Beat Küng
05b0c412c8 sensors: extend module doc a bit 2017-07-14 11:57:11 +02:00
Beat Küng
36c9400de4 gps: use ModuleBase class & add documentation
Note: it changes the interface slightly: instead uf -dualgps, use -e now.

This also fixes 2 bugs:
- nullptr access when doing 'gps status' with fake gps running
- close(fd) was called on an uninitialized fd when gps fake was running
2017-07-14 11:57:11 +02:00
Beat Küng
6463bd4f6f sensors: use ModuleBase & add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
5923a2e9d0 src/mainpage.dox: remove this file, it's not used anymore & completely outdated 2017-07-14 11:57:11 +02:00
Beat Küng
a43f135ad4 minor documentation updates to some commands 2017-07-14 11:57:11 +02:00
Beat Küng
7d50f3df0a Makefile: add module_documentation target 2017-07-14 11:57:11 +02:00
Beat Küng
7a4f557a7a px_process_module_doc: separate page into one page per category 2017-07-14 11:57:11 +02:00
Beat Küng
05c3b711f3 fix bl_update: move definition of print_usage into the ifdef
fixes the compile error:
error: 'print_usage' defined but not used [-Werror=unused-function]
2017-07-14 11:57:11 +02:00
Beat Küng
a4ca3fc607 ver: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
68d754b65e usb_connected: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
8e965a7a2a topic_listener: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
1b4467f674 sd_bench: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
06178392ce reboot: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
16e0e1f7ca perf: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
ba1a483cd6 nshterm: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
65b11d39a9 mtd: add documentation & do cleanup (remove err(), ...) 2017-07-14 11:57:11 +02:00
Beat Küng
e362f760c4 motor_test: add documentation & do cleanup (remove err(), ...) 2017-07-14 11:57:11 +02:00
Beat Küng
4839ed8498 motor_ramp: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
3a880a09d6 mixer: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
b18a148129 led_control: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
50d1ed99b0 i2c commmand: remove errx 2017-07-14 11:57:11 +02:00
Beat Küng
6b99b3412e esc_calib: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
0fdd2b9fea dumpfile: add documentation & do cleanup (remove err(), ...) 2017-07-14 11:57:11 +02:00
Beat Küng
7893623d75 fix dumpfile: specify stack size 2017-07-14 11:57:11 +02:00
Beat Küng
4ea44e51b7 config.c: add documentation & do cleanup (remove err(), ...)
Also changes the order of the arguments for consistency.
2017-07-14 11:57:11 +02:00
Beat Küng
be25c337f9 bl_update: add documentation & do cleanup (remove err(), ...) 2017-07-14 11:57:11 +02:00
Beat Küng
35aa95c25f perf_counter.c: mention that the latency buckets are in us 2017-07-14 11:57:11 +02:00
Beat Küng
872049dc57 pwm.cpp: extend documentation for Oneshot 2017-07-14 11:57:11 +02:00
Beat Küng
fac6a829c4 pwm.cpp: fix issues by clang tidy (nullptr & void) 2017-07-14 11:57:11 +02:00
Beat Küng
37ff267b68 param.cpp: fix issues by clang tidy (nullptr & void) 2017-07-14 11:57:11 +02:00
Beat Küng
b32b0d9b17 hardfault_log: add documentation 2017-07-14 11:57:11 +02:00
Beat Küng
488bc9d7f3 hardfault_log.h: fix comments 2017-07-14 11:57:11 +02:00
Beat Küng
3b0da512a5 px_process_module_doc: add --no-validation flag
and make sure the command failed if there's a validation error.
2017-07-14 11:57:11 +02:00
Beat Küng
d309617998 param.c: rename to cpp and add module documentation
use c++ so that raw string literals can be used
2017-07-14 11:57:11 +02:00
Beat Küng
647bdef855 pwm.c: rename to pwm.cpp and add module documentation
use c++ so that raw string literals can be used
2017-07-14 11:57:11 +02:00
Beat Küng
3f6769d41e uorb: add module documentation 2017-07-14 11:57:11 +02:00
Beat Küng
f25549169c fmu: wait until running, and handle mode_rcin properly
when the fmu was already running in a pwm mode, changing to mode_rcin would
not have any effect.
2017-07-14 11:57:11 +02:00
Beat Küng
3b64be44f4 ModuleBase: add wait_until_running() method 2017-07-14 11:57:11 +02:00
Beat Küng
6778be2c6e mavlink: remove 'p' from px4_getopt()
It is not handled and not documented.
2017-07-14 11:57:11 +02:00
Beat Küng
0909b58981 fmu.cpp: fix wrong command usage mode_pwm3cap2 -> mode_pwm2cap2 2017-07-14 11:57:11 +02:00