37624 Commits

Author SHA1 Message Date
TSC21
162e0c7675 microRTPS: client: reserve the minimum required stack to the send/receive tasks 2020-07-31 14:13:10 +01:00
TSC21
0b41aa3ecd microRTPS: client: dynamically allocate the uORB pub/subs 2020-07-31 14:13:10 +01:00
TSC21
398f104918 microRTPS: transport: do not discard message from rx_buffer if a CRC error occurs 2020-07-31 14:13:10 +01:00
TSC21
1ab193f548 microRTPS: remove the need for the eClock util 2020-07-31 14:13:10 +01:00
TSC21
acc3866ac9 generate_microRTPS_bridge: make sure that the ROS2 version of FastRTPS is grabbed in a colcon build 2020-07-31 14:13:10 +01:00
TSC21
311a8144e1 microRTPS: client: use structs for pub/subs to avoid increasing the stack usage 2020-07-31 14:13:10 +01:00
TSC21
3db9307dfb microRTPS: transport: make seq_number non-atomic 2020-07-31 14:13:10 +01:00
TSC21
08e72b29b3 microRTPS: micrortps_timesync: reduce max RTTI to 50ms 2020-07-31 14:13:10 +01:00
TSC21
c01bcd41f7 microRTPS: minor adjustements so to improve the readings; add more baud rate options
Co-authored-by: Andrew Wedemier <andrew.wedemier@gmail.com>
2020-07-31 14:13:10 +01:00
TSC21
0124ca6e41 microRTPS: add debug verbose option '-v'; use while loop for reads; ease the RTTI check on timesync 2020-07-31 14:13:10 +01:00
TSC21
2f4eff4c38 microRTPS: add possibility to set HW or SW flow control; improve verbosity aesthetics 2020-07-31 14:13:10 +01:00
TSC21
b2845c60d3 microRTPS: move buffer size to transport 2020-07-31 14:13:10 +01:00
TSC21
407bd8860f microRTPS: transport: hotfix to skip data packets that that don't fit the buffer and continue the readings 2020-07-31 14:13:10 +01:00
TSC21
25d2236cce microRTPS: fix FastRTPS version check on agent templates 2020-07-31 14:13:10 +01:00
Daniel Agar
9b12647ac4 px4io: delete broken test and unnecessary limit
- delete broken px4io test and if_test
 - delete px4io limit (a fixed 400 Hz limit was always set at boot)
2020-07-30 10:29:07 -04:00
Koby Aizer
60d767406a PAW3902: document that the driver is also compatible with PAW3903 module 2020-07-30 10:05:49 -04:00
Matthias Grob
a6777e2650 Subscription: correct doxygen comment 2020-07-30 09:56:01 -04:00
Paul Riseborough
77b11129fa
EKF: replacement of covariance prediction autocode with sympy generated output (#870)
* added python script with ekf derivation (WIP)

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* worked on c code auto-generation

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* save before variable name change

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* changed symbol names

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* added codegeneration class

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* improve 3D mag fusion derivation

Signed-off-by: RomanBapst <bapstroman@gmail.com>

* EKF: Extend ekf sympy derivation to include all observation types

* EKF: Add custom ecl::powf function for integer powers

* EKF: Convert ekf covariance prediction to use sympy output

* EKF: Add test program to compare sympy and matlab covariance prediction

Also tests ecl::powf(x,exp) function

* EKF: simplify ecl::powf function

* Generate code to subfolder generated/

* Add printouts for showing code generation progress

* Move generated covariance code to generated folder

* Upgrade code generation to python3

* main.py: Remove unused create_symbols function

& making code more compact

* main.py: move main part into function

* Code generation: fix passing wrong rotation matrix to yaw_observation ()

* EKF: Amend generated code filename for consistency

* Move ecl::powf function test to unit tests

* EKF: Use updated ecl:powf functionality in test program

* Move ecl::powf to utils.hpp

* Update ecl::powf test

* Update output change indication

* test: update expected output for change indicator

* test: update expected output for change indicator again

Co-authored-by: RomanBapst <bapstroman@gmail.com>
Co-authored-by: kamilritz <kritz@ethz.ch>
2020-07-30 12:44:08 +10:00
Daniel Agar
e4fa7597f4
logger: SDLOG_PROFILE remove estimator replay from default to minimize log rate
- log full sensor_combined by default for now
 - small decrease to input_rc rate (manual_control_setpoint is no longer filtered)
 - sensor_correction can be logged at full rate (low publication rate)
2020-07-29 15:07:42 -04:00
Daniel Agar
1b30bd328e logger: decrease try subsribe interval 1000 ms -> 20 ms 2020-07-29 13:36:22 -04:00
Daniel Agar
7b46efaa6b logger: record message gaps 2020-07-29 13:36:22 -04:00
Daniel Agar
f7415c3354 optical_flow/paw3902: silence info output (info -> debug) 2020-07-29 11:58:54 -04:00
Daniel Agar
86365949f6
Update submodule mavlink v2.0 to latest Wed Jul 29 00:38:22 UTC 2020
- mavlink v2.0 in PX4/Firmware (0b2d4a8ae765f36f984e7b6ddd12a7b17b767ed2): f90ef7c95a
    - mavlink v2.0 current upstream: cf6e8cb415
    - Changes: f90ef7c95a...cf6e8cb415
2020-07-28 23:50:02 -04:00
Katrin
a448e82798
Rover Airframe 50004_dfrobot_gpx_asurada: Changing of physical parameter
- the values of the parameters GND_MAX_ANG and GND_WHEEL_BASE are outdated. They belonged to another Rover setup.
 - in the mixer file rover_diff_and_servo.main.mix the steering was controlled by roll, but in PX4 rover steering is controlled by yaw. And this was the reason why the attitude control did not work correctly
 - the DF Robot GPX:Asurada rover has actual a steering angle of 60 degrees. And and wheel base of 0.17m. Parameter values in the airframe file are changed to this values
2020-07-28 21:34:12 -04:00
pengl-aee09
18eccb0cbd PAW3902: align mode change logic with the spec
1. The spec specifies that the mode change condition should be met for 10
   consecutive frames before changing to the next mode.
2. The spec (and comment) says that "PAW3902JF should not operate with Shutter < 0x01F4 in Mode 2" -
   however the if condition checked the reverse condition

Signed-off-by: Koby Aizer <koby.aizer@tg-17.com>
2020-07-28 21:29:43 -04:00
bazooka joe
8a3a71caed simplify the code to calculate signal_quality 2020-07-28 23:45:38 +01:00
bazooka joe
4d1c7b734c don't set quality to 0 for lidar lite v3hp, because the strength data is valid even for short distance 2020-07-28 23:45:38 +01:00
Matthias Grob
0bffd951ec AlphaFilter: include float.h for FLT_EPSILON 2020-07-28 15:41:58 -04:00
Daniel Agar
ca33bb1c01
load_mon: slightly longer cpu average (300 -> 500 ms) 2020-07-28 13:41:50 -04:00
Julian Oes
b108adc5f1 Tools: retry gz model if gzserver is not ready yet
This should prevent the race between gzserver and gz model and fix the
integration tests which sometimes timeout because the model is not
spawned correctly.

This patch also changes the shebang to what's generally recommended.
2020-07-28 11:51:51 +02:00
stmoon
71b7647ca1 fix the return type problem of RTPS 2020-07-27 16:22:46 +01:00
stmoon
b457122489 remove unnecessary stderr msg when checking ldconfig 2020-07-27 16:21:58 +01:00
kritz
88c52aba5e
Refactor ev fusion start into helper functions (#872) 2020-07-27 11:42:52 +02:00
Daniel Agar
7354e39893
Jenkins HIL remove mRo Control Zero
- there are issues with the particular harware on the rack (an early prototype)
2020-07-26 19:36:44 -04:00
Daniel Agar
cfbf69f2a7
boards: rename Hex -> CubePilot
- hex_cube-orange_default -> cubepilot_cubeorange_default
 - hex_cube-yellow_default -> cubepilot_cubeyellow_default
2020-07-26 13:55:41 -04:00
kamilritz
8c65ca29e4 Only run firmware build test on pull_request 2020-07-26 10:11:52 -04:00
kamilritz
049f59d7de Fix firmware-build-test 2020-07-26 10:11:52 -04:00
Daniel Agar
62fe6d59cc
boards: hex cube yellow fix STM32F7 selection (STM32F765II -> STM32F777VI) 2020-07-24 12:03:25 -04:00
Hamish Willee
4ade24869f
parameters: move XML injection to the group level (#15403)
So that they are also in the markdown and json output.
2020-07-24 13:45:53 +02:00
Matthias Grob
400d97e60c math: add unit tests for everything in Functions.hpp 2020-07-24 11:31:15 +02:00
Matthias Grob
0b391fdcfc mc_att_control: add gradual3 function to cover hover thrust rescaling 2020-07-24 11:31:15 +02:00
Daniel Agar
aa7735c1c0 pwm_out: limit actuator control callbacks to primary groups
- add backup schedule at minimum PWM rate
 - fixes #15043
2020-07-23 09:45:04 -04:00
Daniel Agar
0586079a84 mixer_module: add subscription option to limit additional actuator_control callbacks
- optionally only register callbacks for primary control groups (if used)
2020-07-23 09:45:04 -04:00
Daniel Agar
9426c68a13 cmake: only allow gold linker for posix builds
- the gold linker doesn't currently work for NuttX builds
 - NuttX skip --print-memory-usage if using the GOLD linker
 - fixes #15400
2020-07-23 09:41:35 -04:00
Mirko Denecke
7ac66bae4f hex io firmware remove double definition of GPIO_HEATER_OFF 2020-07-23 09:41:05 -04:00
Mirko Denecke
b7389119b3 px4 io firmware remove double definition of GPIO_HEATER_OFF 2020-07-23 09:41:05 -04:00
Julian Oes
26021b01cb Tools: abort SITL start if gzserver fails
Sometimes gzserver seems to not start or not start fast enough. In this
case, instead of stalling forever, it would be nice to abort.
2020-07-23 07:42:09 +02:00
Mirko Denecke
01e9599e93 HEX Cube Yellow: enable platform-specific IO firmware with inverted heater pin. 2020-07-22 10:50:47 -04:00
Mirko Denecke
44e2c326e0 HEX Cube Orange: enable platform-specific IO firmware with inverted heater pin. 2020-07-22 10:50:47 -04:00
Mirko Denecke
57968c6e27 Add platform-specific IO firmware for HEX autopilots. 2020-07-22 10:50:47 -04:00