David Sidrane c8bd60bef8 Mpu9250:Allow internal reset to complete, when started from VDD of 0V
Per the data sheet: Start-up time for register read/write from power-up is
   Typically 11 ms and the Maximum is 100 ms.

   It seems the power up reset is only triggered at VDD < 150 mV. So the
   symptom reported: Failure is only happening after a long power down is
   consistent with VDD not dropping below 150 mV, therefore not generating
   a POR and being ready to be written with out delay.

  This fix adds a delay of 110 ms to ensure the reset has ended with some.
  margin.
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PX4 Pro Drone Autopilot

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Slack Gitter

This repository holds the PX4 Pro flight control solution for drones, with the main applications located in the src/modules directory. It also contains the PX4 Drone Middleware Platform, which provides drivers and middleware to run drones.

Please refer to the user documentation and user forum for flying drones with the PX4 flight stack.

Weekly Dev Call

The PX4 Dev Team syncs up on a weekly dev call.

Developers

Maintenance Team

Supported Hardware

This repository contains code supporting these boards:

Project Milestones

The PX4 software and Pixhawk hardware (which has been designed for it) has been created in 2011 by Lorenz Meier.

Description
a mirror of official PX4-Autopilot
Readme BSD-3-Clause 587 MiB
Languages
C++ 51.2%
C 38.5%
CMake 4.7%
Python 3.9%
Shell 1.3%
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